Getting Ready To Go

Been a while since the last post, but been spending time getting ready for the big trip.  In October, 2011, Ann and I leave for Baja where we’ll spend a couple months, then in March, 2012 we’ll leave for French Polynesia.  Don’t have a firm plan yet, just know we’re leaving and once we get there we’ll see how long we want to stay.

So, in preparation it’s been a busy Spring and Summer:

  • Put in a Spectra Watermaker (pic below)
  • Hauled and painted the bottom
  • Put in a Frigoboat refrigerator (pic of Keel Cooler, the bronze looking thing, below)
  • Bought a new boom (the old one had a permanent bend and was looking like it was getting ready to break.  Ballenger Spars made a new custom one)
  • Took the Cetol off the teak cockpit seats/floor with a heat gun.  The Cetol was waaaay too slippery when wet.  Took two days, but result was excellent.  Now I just have to bleach the wood, sand a bit and recaulk a couple seams and we’re good to go.
  • Bought a new “blue water” fishing pole and reel.  The other one was too small for the kind of fish we were hooking.

Those are the “big ones” and my wallet is lighter, but Charisma is happy.
Also got some brand new storm sails, wheels for the dinghy (to make it easier to haul up on shore) and a bunch of smaller projects to get ready to go.  We’re now in full speed ahead mode with about one month to go before we leave.

Still to come:

  • Solar panels that I will hang on the lifelines/rails
  • A water generator.  Ferris makes a unit you can tow behind the boat.  A small prop and 75 feet of torque-rope and it turns a small generator that puts out quite a lot of electricity for the batteries.  Great for tradewind sailing.

Well, that’s it for this catch-up note.  The blog’s gearing back up.  Keep in touch!

polishing-the-topsides.jpg

keelcooler.jpg   watermaker.jpg

WATER AN INCH BELOW THE FLOORBOARDS!!

The blood in my veins ran cold. We had some rough weather all night and were finally just 20 miles off San Diego when something told me to go check the bilge. When I opened a floorboard the shock of seeing water sloshing against the bottom of it gripped me by the throat.  I knew Charisma has a four foot deep bilge, so water within an inch of the top was a LOT of water. Instantly I pulled off the rest of the floorboards exposing the manual bilge pump and started pumping like hell.  Almost right away it jammed.  A problem I was having as I tested it two months ago before leaving, but I thought it was solved. There had been a lot of shavings and junk in the bilge and the filter kept jamming.  I had cleaned it six times while in Berkeley and it seemed to have cleaned the bilge out, but now the same problem again.  Probably two months of sailing and some small sloshing had dislodged more “gunk”.  I ran to the electric bilge pump and turned it on.  It started running, but watching the bilge, there seemed to be no reduction in water.  I could hear that it was primed and pumping, but not fast enough!!  That possibly meant a BIG leak.

Quickly now, my only alternative was to tear down the filter to the big pump and clean it.  Jumped to it, cleaned, put back together, pump more.  Air was leaking through the filter so the pump wasn’t working.  Broke down the filter again, cleaned the gaskets and back together.  Some air still leaking, but pump working to about half capacity.  Now I’m pumping for all I’m worth and envisioning evacuating the boat into the liferaft I had bought but never intended to actually use.  Thinking my arm is now getting really tired and sore and I’m not sure how much arm strength I’m going to have left, and then I noticed that the water was slowly decreasing.  Yes, definitely getting lower.  I’m making progress!  Another couple minutes and I finally heard that awesome (at this point) sound of the pump pulling only air.  The bilge had emptied.  For now.  Watching deep into the bilge for more water coming in I saw none.  Hmmm.  A mystery.  Looks like we’re not sinking, at least for now.

With a reprieve, I took apart the filter in the large manual pump more thoroughly, especially the gaskets which seal it from air being sucked in and put that back together for the fourth time.  Another look in the bilge, still no more water, so I can finally relax a bit and really start looking around inside the boat to see what the water damage might be.  Turned out we had been on starboard tack all the time so it was the port side that received the water (not the starboard side where my clothes drawer is!)  Unfortunately the port side is where a lot of the food is stored near the floor.  Oops.  Pulled up the cushions looked under the seat into the big bins and…oh yeah, water got in here big time.  Soaked all the vegetables and other stuff, but fortunately most of it was sealed in plastic.  Tortillas, crackers, cereal, rice, pasta and other such “long term” stuff were all protected.  In fact the only casualty was a box of macaroni that had soaked through and “sloshed” its way through the food locker with some no doubt making it to the bilge.  OK, clean the locker, dry the veggies (turned out this didn’t matter too much as most of the citrus, miscellaneous vegetables and apples were confiscated by customs in San Diego a little later that day).

OK, clean up done, still no water in the bilge, time to find out how the heck somewhere in the neighborhood of 100 or so gallons of water made it into the boat.  Boats are supposed to keep this much water OUTSIDE.  Started the mental checklist; chainplates, toe rail, deckplates…too small… anchor hawsepipes… (!!!)  Ah ha, maybe the little holes where the chain went through the caps were sucking down water when we were burying the bow in the big waves all night.  I went forward to have a look and found it big time.  The port anchor chain hawsepipe had been knocked completely off leaving a gaping four inch hole right down into the chain locker with subsequent draining into the bilge.  Yipes.  How did that happen?  Every wave must have dumped a couple gallons of water as the bow went under.  A closer look revealed that the foot or so of chain running along the deck from anchor into the pipe had been getting knocked around by the big waves (I saw chafe on the deck) and finally one wave must have bumped it so hard it knocked the cover up and off.  Actually a big relief to discover the problem.  Now I can fix it and not worry about some invisible leak in the boat.  I have now put a clip on the cover and attached it to a couple feet of chain hanging into the locker, so it’s now weighed down pretty well.  I might yet also put a pin on it when I get back, but that should work for now, especially if I check it periodically if we get into some big seas again.

I think I’ve just found out what they say; “you can never have enough bilge pumps”.

Work in Paradise

Yup, today was a workday.  Since we’re officially halfway on our voyage, mileage-wise at 1752 miles, it was time for some boat maintenance before we leave tomorrow to begin our trip back. Actually, we’re not heading “back” for a few more days, as the next two or three days will be at Islas Espiritu Santos, about 20 miles East of La Paz.

Technicalities of the trip aside, there was work to do.  Charisma badly needed a fresh water wash, not having seen same since San Francisco.  She is much better now thank you very much.  I even thing she’s smiling now that all the salt has been rinsed off.

Down below, I changed the oil, oil filter, and the primary and secondary fuel filters.  Diesels will run forever IF they have clean fuel and oil (knock on wood).  We have used 114 hours since leaving SF on the engine.  Most of those hours have been “easy” hours used to run the alternator to refresh the batteries for power for nav instruments and lights, but as we move up the Sea of Cortez, we do less sailing and more motoring (less wind and when we have it, it’s right on the nose), so at least 20 of those hours have been in the last week.  We did very little motoring from SF all the way to Cabo.

Geoff started the day by going to the Mercado.  He had a fun time getting supplies and returned with stories of how to butcher a pig (apparently today was “pig day” at the market) as well as lots of fresh vegetables which down here means various peppers, some tomatoes, avocados, limes and sweet potatoes.  We stripped all the cardboard off, washed all cans and fresh veggies in white wine vinegar (the object is to wash/kill any pest eggs) and then stored all the provisions.  Hopefully this will keep Charisma pest free.

Geoff also made the supreme mistake of asking; “what else can I do?”  The Supreme Commander (yes, I still wear that hat occasionally) with an evil glint in his eye innocently said; “the ice boxes could use washing down”.  In reality, the Supreme Commander had discovered earlier, while changing the oil, the source of flies in the boat. They appeared to come from some fish that had gone bad a couple weeks ago and which run-off found its way into the bilge (the iceboxes drain there).  This resulted in maggots in the bilge, etc, etc.  The upshot: Geoff cloroxed the heck out of the ice-boxes, the drains into the bilge and the bilge itself.  All mentioned are now so clean, we could drink out of them.  In fact, after pumping the bilge, I think the marina is pretty clean now too!  The flies persist, but we’re eliminating them one at a time.  Not all is paradise in paradise.

For my part, I made a smallish mistake.  I decided that the best way to completely clear the bilge was to use the hand pump under the cabin sole.  It drains the bilge completely, whereas the electric pump stops a little short of clearing the bilge.  Anyway, as I said, I wanted to drain the bilge to get rid of the maggots.  The problem is or should I now say; “was”, we also use the manual bilge pump to pump out the holding tank at sea (for landlubbers, it’s where we – well – in the marina – well, it really stinks when we have to pump it out!  OK, I’m not admitting to anything here, I’m just saying; once I cleared the bilge, I had to leave the area for a while as I didn’t want to have to answer any questions from our neighbors or the dock police.  Back at the boat a half hour or so later, there appeared to be no repercussions.

We also discovered that Geoff is excellent at killing flies and bees.  For some reason, some bees had decided that Charisma was a good place to nest.  Probably the cereal Geoff brought back attracted them.  We weren’t as comfortable with them as they seemed to be with us.  Deadly force was exercised.  With dispatch!  The bees have retreated for now.

Boat projects have a way of expanding.  I won’t bore you with all of them, but suffice to say there were a ton of; “tighten this, fix that, etc, etc” and before I knew it, it was MARGARITA TIME.  Geoff is back in town for the evening and I went to the Beach Club for a shower (probably the last one for a while) and a cocktail overlooking La Paz Bay at sunset.  Beautifull!  Then treated myself to a last dinner ashore. I had Carpaccio de Salmone and Salad Rustico or something like that.  My waiter was the highlight:
Omar Fabian Hernadez Mondragon.  He was very, very good.  Really knows his wines and is trying to get into an exchange program to work in Canada.  I gave him my email address and told him I’d be an enthusiastic reference for him.  He seemed genuinely pleased.  My Spanish and his English made conversing an experience!  I hope I didn’t tell him by accident that he could bring his family and live with me in San Francisco.

Opps, almost forgot to mention that in the middle of all the work-Geoff made some excellent fish tacos from the Mahi we caught a couple days ago.  Fresh tortillas, avocados, peppers, salsa, mahi, onions∑.  We’ve been carefully keeping the Mahi and the two tunas on ice, so they are fresh as can be.  Yum.

So, tomorrow, we get up at a reasonable mid-morning hour, motor to the harbormaster and check out.  By then (late morning) hopefully the wind will kick up a bit and we’ll sail the 15 or 20 miles to our next destination.  We’ll see where the weather allows us to anchor (many of the bays at Isla Espiritu Santos are exposed to NW wind).

More once we get there.

Four Days…

Big day today; five hours of varnishing (Cetol) and then finished installing the new Starter Battery.  The last two big projects.  Still need one more coat of Cetol, but a big step to get this one on.  The fiberglass project for the starter battery went great.  The platform I made is very solid.  The battery fits right in a new box and I fabricated some 1/0 wire (that’s about 3/4″ thick wire) to connect it.  Had a couple hiccups with some bizarre previous wiring that I had to figure out to make it all work, but work it does.  Connected the new starter battery to a Xantex Echo Charger.  In short: it lets the house bank charge up first and then automatically turns on and charges the starter battery.  Tested it with both the AC charger (the 110 volt line from the dock) as well as from the engine just using the alternator.  Appears to work in both modes.  On another note:  PARTY ON FRIDAY!  We’re going to have an Bon Voyage party at the boat Friday night.  Ann’s son, Andy is nice enough to volunteer to come down and man the BBQ.  Beer and meat products.  Yay!  Probably won’t have everything I want done, but even if I had another month, I’d likely find more stuff to do and wouldn’t feel like I was done.  Just time to GO!

Five days and counting…

We’ve leaving for San Diego and then Baja in five days.  Tons of work done and a fair amount still to do, but manageable.  Still need a couple coats of Cetol on the rails, but other than that, we’re about set other than food.  Still some details though, the biggest one is that I decided at the last minute to add a starter battery.  Ordered an “echo charger” which should arrive tomorrow (Monday).  Bought the battery and fabricated a platform out of wood and fiberglassed it in today.  Will check tomorrow and see if it it strong enough.  So, here’s what we’ve gotten done:  Cleaned out all the “liveaboard stuff” and moved it to the storage unit.  Brought 130 jib, asym, dinghy and engine down to the boat.  Been playing in the dinghy all day to AHEM make sure it’s working effectively.  Taped off the rails so I can start final Cetol coats Monday and Tuesday.  Already put two to three coats on everything else.  Rigged two new hatch scoops (to bring air into the hatches in the tropical climes.  Bleached the iceboxes and storage bins to make sure they are clean, bought and working on installing boards to hold 10 gallons of potable water and 10 gallons of diesel on the foredeck for emergency use and about fifty other small but necessary projects that each take up time and energy.  Fun though, knowing that you’re going to be self-sufficient and need to have everything in working order.  Here’s a couple pics of our Baja crew and flag.It’s “HaHa” time     The Motley Crew

Countdown to Baja: 14 Days!

It’s getting real.  Only two weeks left.  This weekend with Ann’s help we completed the following:  Varnished the brightwork on the cabin top, fixed the manual bilge pump including installing a new section of hose (problem was a jammed filter.  Flushed and cleaned it several times), pulled all the chain out of the stb’d anchor and all the rope out of the port anchor and labelled every ten feet, changed the oil and the oil and fuel filters on the engine.  Good effort.  Some more stuff to go, but getting there.Varnish Time     Floorboards up     In the bilge

Transmission’s Broke

Yup, that’s what the mechanic said.  Went out for a sail on coming into the harbor on the way back the engine started making “expensive” noises.  You know, the screeching, grinding ones.  I initially thought it was the fresh water pump, but when I took off the fan belt and tugged on the pump shaft it was tight and spun freely.  Started the engine again and realized it was coming from the transmission area.  Time to call in the mechanic.  He immediately diagnosed it as a broken stress plate spring.  Turned out that was close.  It was the fan on the stress plate that broke.  Pieces were flailing around inside the bell housing.  The “tranny” was fine, but the stress plate was toast.  We pulled the bell housing, took off the stress plate and it turned out the flywheel had to come out too due to some bolts on the stress plate corroding onto the flywheel.  A week later and a new stress plate and we’re back in motion (oh, and about $1500!)                The stress plate      The broken part     Sending the tranny out for cleaning

Boatwork Week

Took a week off to get some work done.  Wanted to do some varnishing (OK, “Cetoling”), but the weather wasn’t cooperating.  Fog and threat of rain.  Instead did a bunch of the “little” projects that are always on “the list” but don’t get done.  Biggest among these was the dreaded chainplate sealing.  Taking the deck covers off the chainplates, digging out the old bedding compound and resealing all.  Takes about an hour per chainplate times four!  Backbreaking, as you are on hands and knees removing screws, prying covers off the deck, digging out old bedding, etc.Chainplate projectAlso removed and replaced the anchor washdown pump.  I had “fixed” the old pump that had seized, but it seized again and I decided just to buy a new one.  However, it sat on the “to do” list for about six months since it wasn’t a big priority.  When I finally got to it this week, it took about an hour and a half.Pump located near the mast step     Changing the new pumpSome other small but important stuff:  Bringing my collection of flares up to date.  Now I’m legal till 2013 (but what do I do with the other 15 year old flares?).  Taking all three fire extinguishers for pressure testing, reloading and re-certification.   Now Charisma’s 100% legal if stopped for inspection by the Coasties.Also, fixed the head which again broke.  This time the water inlet refused to work.  As I thought, it turned out to be the float valve.  Took off the bowl, “jiggled” the float ball, reassembled and voila, it works!  Nice to be able to pump water again and not have to pour fresh water into the bowl to flush.

Dreaded Maintenance

Yep, the complete disassembly of the toilet!The head over a period of months was having a harder and harder time pumping out.  Finally it stopped flushing, so no other alternative other than taking it completely apart to find out the mystery of the marine head.I've never taken one apart or seen one taken apart, so this was completely new territory.  I removed the intake and discharge hoses (yuck), and rubber-banded a plastic bag over the discharge side since it went directly into the holding tank.  Then unbolted the head from the floor and took it outside into the cockpit for further disassembly.Once completely taken apart, the problem become apparent.  There's a rocker valve that pushes a float ball up to seal the air into the toilet that allowed the pump to go from pulling water into the bowl to sealing it and pumping water out.  The rocker had a set screw that had come loose, which allowed the rocker to slip.  Hence the whole discharge function stopped functioning!OK, $80 worth of parts from Groco later and I was ready to reassemble.  (As a brief aside: the Groco rep I talked to on the the phone was the person who actually built my toilet back in 1998!  Talk about customer service).Everything went back together quite easily with the exception of a leaky gasket.  In plumbing there's always a leaky gasket!  In this case, it was the gasket that linked the toilet bowl to the base. I had tightened it too much as is often the case in plumbing problems.  Once you over-tighten a gasket, it collapses and you're out of luck.  I took the bowl off-worried that I had broken the porcelain by overtightening, but hadn't-removed the gasket, cleaned it and put it back on.  Then reassembled the bowl "loosely" this time.  Re-attached the intake and discharge and pumped.  Leaking.  Tighten the bowl a little.  Still leaking.  Tighten a little more.  Leaking, but a little less. Tighten a liiiittttlee more.  Leak stopped.  It's a fine line.Toilet works better than ever and leak has stopped.   All in all, not as bad as I thought it would be and another adventure complete!Lots of parts!      The bowl, the base (upper right) and parts in a bucket

Bottom Job

Well, it sounds a bit more “interesting” than the reality.  It’s been 20 months since Charisma was hauled out and the bottom painted.  Last time I noted that the bottom paint had not been stripped in many years and was looking like it needed to be completely removed.  The problem was the price.  A certain boatyard in Alameda that starts with an “S” quoted over $10K to do it.  They didn’t really want to do it and recommended; “go to Mexico and get it done there”.  Hmm.  When I hauled this time at KKMI (a great boatyard) they quoted substantially less to strip all the paint and put on two new epoxy coats and two anti-fouling coats.  They have a technique called soda-blasting.  High pressure baking soda.  Takes offthe paint, but not the gelcoat.  Less damage to the boat means less labor.     Tented and ready to go     In the space-suit     Down to the gel-coat     Polishing the hull  While she was hauled I also spent a “fun” 8 hours polishing the topsides.  Lot of work, but she looks nice! Oh yeah, and as with most projects, there was a surprise.  I’ve had a problem with the raw water pump losing prime when idling for long periods at very low rpm.  The engine guy at KKMI told me he felt the pump was worn out.  “Take it out and show it to me and I’ll tell you”.  So out came the old pump and sure enough, the brass collar around the impeller was worn down and not compressing the blades far enough.  $900 later I had a new pump, which I installed.  Works great.  Lots more water pressure coming out the exhaust too.The old pump  The new paint job has resulted in almost a Knot of boat speed.  I guess the old paint which was peeling and not smooth anymore was slower than I thought!